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Difference between revisions of "34-121-23008"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-121-23008
 
| Well ID: 34-121-23008
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.6200911247, -81.5414703424 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.62021679, -81.54207287 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Noble County, Ohio|Noble]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[BENATTY CORP
 +
]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1983-09-20
 
| Spud Date: 1983-09-20
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
| Violations: 4
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.6200911247
+
| Latitude: 39.62021679
 
|-
 
|-
| Longitude: -81.5414703424
+
| Longitude: -81.54207287
 
|-
 
|-
 
|}
 
|}
Line 43: Line 44:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 19836.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 8695.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 5089.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 5887.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 3552.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 3808.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 3288.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 3312.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 2064.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 36.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 1980.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 2223.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 2676.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 2161.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 1938.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 1376.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 56.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 1303.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 867.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 36.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 128.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 24.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 275:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 1132488629
 
| 1132488629
 
| 2005-11-18
 
| 2005-11-18
|
+
|  
 
| Upon inspecting well site found well to be idle at this time no I.D. posted no production chart could be found,will need to call company and inquire about well status!
 
| Upon inspecting well site found well to be idle at this time no I.D. posted no production chart could be found,will need to call company and inquire about well status!
|
+
|  
|
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| 1173397479
+
| 1132488629
| 2007-03-08
+
| 2005-11-18
|
+
|  
| Upon inspecting well site again found well still idle all valves at wellhead are shut slight odor of H2S gas noted well is equipped with 8" surface casing and 4.5" production casing and 1,5" tubing and 1-210 bbl tank and 1-rotted out 50 bbl tank and separator, no I.D. posted and last production reported was in 2004,talked to Jeff Marshall concerning well on a couple occasions with no results in getting well back into production.
+
| Upon inspecting well site found well to be idle at this time no I.D. posted no production chart could be found,will need to call company and inquire about well status!
|
+
|  
| 9-9-05(A)10
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1173397479
 
| 1173397479
 
| 2007-03-08
 
| 2007-03-08
|
+
|  
| Upon inspecting well site again found well still idle all valves at wellhead are shut slight odor of H2S gas noted well is equipped with 8" surface casing and 4.5" production casing and 1,5" tubing and 1-210 bbl tank and 1-rotted out 50 bbl tank and separator, no I.D. posted and last production reported was in 2004,talked to Jeff Marshall concerning well on a couple occasions with no results in getting well back into production.
+
| Upon inspecting well site again found well still idle all valves at wellhead are shut slight odor of H2S gas noted well is equipped with 8 surface casing and 4.5 production casing and 1,5 tubing and 1-210 bbl tank and 1-rotted out 50 bbl tank and separator, no I.D. posted and last production reported was in 2004,talked to Jeff Marshall concerning well on a couple occasions with no results in getting well back into production.
|
+
|  
| NONE
+
|  
|
+
|  
|-
 
|-
 
| 1181777328
 
| 2007-06-13
 
|
 
| No change in status of well it is still idle,talked to company rep stating that well would be plugged this summer as soon as service rig ecame available.
 
|
 
| 9-9-05(A)10
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1181777328
 
| 1181777328
 
| 2007-06-13
 
| 2007-06-13
|
+
|  
 
| No change in status of well it is still idle,talked to company rep stating that well would be plugged this summer as soon as service rig ecame available.
 
| No change in status of well it is still idle,talked to company rep stating that well would be plugged this summer as soon as service rig ecame available.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1184888519
 
| 1184888519
 
| 2007-07-17
 
| 2007-07-17
|
+
|  
 
+
| Request from well owner too assist in locating well and try and determine lease road entry located well and and took H2S  gas check noted odor but detector didn
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1185015439
 
| 1185015439
 
| 2007-07-18
 
| 2007-07-18
|
+
|  
 
| On site to witness operator attempt to free up tubing no success call out logging truck to perf tubing to set bottom hole plug (perfed@5450') then determined free pt of tubing@4000' (shot off) then pulled tubing and ran in hole with rip tool to determine free pt of casing to set required plug.
 
| On site to witness operator attempt to free up tubing no success call out logging truck to perf tubing to set bottom hole plug (perfed@5450') then determined free pt of tubing@4000' (shot off) then pulled tubing and ran in hole with rip tool to determine free pt of casing to set required plug.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1185227991
 
| 1185227991
 
| 2007-07-23
 
| 2007-07-23
|
+
|  
 
| Well has been plugged resolving previous NOV.
 
| Well has been plugged resolving previous NOV.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1395614580
 
| 1395614580
 
| 2008-07-07
 
| 2008-07-07
|
+
|  
 
| Final restoration work at site satisfactory,pit has been filled in and site restored and vegetation has been established.
 
| Final restoration work at site satisfactory,pit has been filled in and site restored and vegetation has been established.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| PL7689
 
| PL7689
|
+
|  
|
+
|  
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 04:28, 15 July 2015

Well Details

Well ID: 34-121-23008
Loading map...
County: Noble
Municipality:
Operator Name: [[BENATTY CORP

]]

Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1983-09-20
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.62021679
Longitude: -81.54207287

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 19836.0 0.0
1985-0 8695.0 0.0
1986-0 5089.0 0.0
1987-0 5887.0 0.0
1988-0 3552.0 0.0
1989-0 3808.0 0.0
1990-0 3288.0 0.0
1991-0 3312.0 0.0
1992-0 2064.0 36.0
1993-0 1980.0 0.0
1994-0 2223.0 0.0
1995-0 2676.0 0.0
1996-0 2161.0 0.0
1997-0 1938.0 0.0
1998-0 1376.0 56.0
1999-0 1303.0 0.0
2000-0 867.0 0.0
2001-0 36.0 0.0
2002-0 128.0 0.0
2003-0 24.0 0.0
2004-0 0.0 0.0
2005-0 0.0 0.0
2006-0 0.0 0.0
2007-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1132488629 2005-11-18 Upon inspecting well site found well to be idle at this time no I.D. posted no production chart could be found,will need to call company and inquire about well status! Compliance Notice
1132488629 2005-11-18 Upon inspecting well site found well to be idle at this time no I.D. posted no production chart could be found,will need to call company and inquire about well status!
1173397479 2007-03-08 Upon inspecting well site again found well still idle all valves at wellhead are shut slight odor of H2S gas noted well is equipped with 8 surface casing and 4.5 production casing and 1,5 tubing and 1-210 bbl tank and 1-rotted out 50 bbl tank and separator, no I.D. posted and last production reported was in 2004,talked to Jeff Marshall concerning well on a couple occasions with no results in getting well back into production.
1181777328 2007-06-13 No change in status of well it is still idle,talked to company rep stating that well would be plugged this summer as soon as service rig ecame available.
1184888519 2007-07-17 Request from well owner too assist in locating well and try and determine lease road entry located well and and took H2S gas check noted odor but detector didn
1185015439 2007-07-18 On site to witness operator attempt to free up tubing no success call out logging truck to perf tubing to set bottom hole plug (perfed@5450') then determined free pt of tubing@4000' (shot off) then pulled tubing and ran in hole with rip tool to determine free pt of casing to set required plug.
1185227991 2007-07-23 Well has been plugged resolving previous NOV.
1395614580 2008-07-07 Final restoration work at site satisfactory,pit has been filled in and site restored and vegetation has been established.
PL7689 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.