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Difference between revisions of "34-083-24402"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-083-24402
 
| Well ID: 34-083-24402
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.2421952359, -82.3315662544 | width=100% | height=100% }}
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| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.24219524, -82.33156625 | width=100% | height=100% }}  
 
|-
 
|-
| County:
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| County: [[Knox County, Ohio|Knox]]
 
|-
 
|-
| Municipality:
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| Municipality:  
 
|-
 
|-
| Operator Name:
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| Operator Name: [[E & C MILLER PRODUCTIONS LLC]]
 
|-
 
|-
| Well Pad ID:
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| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
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| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
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| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
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| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2008-08-15
 
| Spud Date: 2008-08-15
 
|-
 
|-
| Unconventional:
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| Unconventional: No
 
|-
 
|-
| Horizontal:
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| Configuration: Vertical
 
|-
 
|-
| Producing: No
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| Well Status: Dry and Abandoned
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 40.2421952359
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| Latitude: 40.24219524
 
|-
 
|-
| Longitude: -82.3315662544
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| Longitude: -82.33156625
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -1844793281
 
| 2008-08-25
 
|
 
| Jeff Fry and I inspected well drilling operation today.  Larry King is rigged up and drilling at 88 feet.  The surface string is on location.  He has the permit on location and there is a lined pit.  No violations noted this date.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1220620329
 
| 1220620329
 
| 2008-09-05
 
| 2008-09-05
|
+
|  
 
| Witnessed mudding of 340 ft of 5 inch surface casing .
 
| Witnessed mudding of 340 ft of 5 inch surface casing .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1221563801
 
| 1221563801
 
| 2008-09-15
 
| 2008-09-15
|
+
|  
 
| Still working on completion of mudding surface casing. Pipe is tight, fluid to approx. 30 ft. Discussed with J Fry and decided to allow bentonite and clay to be used to finish topping off. 4 tons of bagged clay already used.
 
| Still working on completion of mudding surface casing. Pipe is tight, fluid to approx. 30 ft. Discussed with J Fry and decided to allow bentonite and clay to be used to finish topping off. 4 tons of bagged clay already used.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1221846511
 
| 1221846511
 
| 2008-09-19
 
| 2008-09-19
|
+
|  
 
| Vern finished topping off surface job with 6 bags of bentonite clay and 200 # of fireclay. The clay held at top. Drilling is now at 550 ft.
 
| Vern finished topping off surface job with 6 bags of bentonite clay and 200 # of fireclay. The clay held at top. Drilling is now at 550 ft.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1222776706
 
| 1222776706
 
| 2008-09-29
 
| 2008-09-29
|
+
|  
 
| Attempt at Berea well was a dry hole. The Millers have decided to plug the well and may reopen some time to attempt a Clinton well. I witnessed part of the bottom plugging today and the first joint of 5 inch was pulled.
 
| Attempt at Berea well was a dry hole. The Millers have decided to plug the well and may reopen some time to attempt a Clinton well. I witnessed part of the bottom plugging today and the first joint of 5 inch was pulled.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1844793281
 +
| 2008-08-25
 +
|
 +
| Jeff Fry and I inspected well drilling operation today.  Larry King is rigged up and drilling at 88 feet.  The surface string is on location.  He has the permit on location and there is a lined pit.  No violations noted this date.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 59725537
 
| 59725537
 
| 2008-08-27
 
| 2008-08-27
|
+
|  
 
| Larry King is still in process of drilling this Berea Well.  Nobody was on location.  No violations noted this date.
 
| Larry King is still in process of drilling this Berea Well.  Nobody was on location.  No violations noted this date.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 03:26, 15 July 2015

Well Details

Well ID: 34-083-24402
Loading map...
County: Knox
Municipality:
Operator Name: E & C MILLER PRODUCTIONS LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2008-08-15
Unconventional: No
Configuration: Vertical
Well Status: Dry and Abandoned
Violations: 0
Latitude: 40.24219524
Longitude: -82.33156625

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1220620329 2008-09-05 Witnessed mudding of 340 ft of 5 inch surface casing .
1221563801 2008-09-15 Still working on completion of mudding surface casing. Pipe is tight, fluid to approx. 30 ft. Discussed with J Fry and decided to allow bentonite and clay to be used to finish topping off. 4 tons of bagged clay already used.
1221846511 2008-09-19 Vern finished topping off surface job with 6 bags of bentonite clay and 200 # of fireclay. The clay held at top. Drilling is now at 550 ft.
1222776706 2008-09-29 Attempt at Berea well was a dry hole. The Millers have decided to plug the well and may reopen some time to attempt a Clinton well. I witnessed part of the bottom plugging today and the first joint of 5 inch was pulled.
-1844793281 2008-08-25 Jeff Fry and I inspected well drilling operation today. Larry King is rigged up and drilling at 88 feet. The surface string is on location. He has the permit on location and there is a lined pit. No violations noted this date.
59725537 2008-08-27 Larry King is still in process of drilling this Berea Well. Nobody was on location. No violations noted this date.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.