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Difference between revisions of "34-079-20250"

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Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-079-20250
 
| Well ID: 34-079-20250
| style="height=100%; align=center" rowspan="15" | {{#display_map: 38.9365584266, -82.622926928 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 38.93655532, -82.62313394 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Jackson County, Ohio|Jackson]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[GEOPETRO LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1995-03-05
 
| Spud Date: 1995-03-05
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 7
+
| Violations: 0
 
|-
 
|-
| Latitude: 38.9365584266
+
| Latitude: 38.93655532
 
|-
 
|-
| Longitude: -82.622926928
+
| Longitude: -82.62313394
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 6576.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 1334.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 79.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 2752.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 507.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 3071.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 148:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
| -243948692
+
| 1054401633
| 2006-05-26
+
| 2003-05-31
|
+
|  
| Gate valve appears to be closed.
+
| received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted.
|
+
|  
| NONE
+
|  
|
+
|  
|-
 
|-
 
| -478273780
 
| 2008-01-29
 
|
 
| No id. Well is capable of production. Lines are connected to the wellhead. Valves are open. Equipment looks new. Site has been mowed and is clean.
 
|
 
|
 
|
 
|-
 
|-
 
| -71065851
 
| 2006-05-26
 
|
 
| FOLLOW UP TO NOV #  -243948692  Gate valve appears to be closed.
 
|
 
| NONE
 
|
 
|-
 
|-
 
| -737133283
 
| 2008-01-31
 
|
 
| Called company and informed them that they need an Id on the well.
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1054401633
 
| 1054401633
 
| 2003-05-31
 
| 2003-05-31
|
+
|  
| received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2" valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2" bull plug and installed as tight as possible with 12" wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted.
+
| received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted.
|
+
|  
| 9-9-05(A)1
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
 
| 1054401633
 
| 1054401633
 
| 2003-05-31
 
| 2003-05-31
|
+
|  
| received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2" valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2" bull plug and installed as tight as possible with 12" wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted.
+
| received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted.
|
+
|  
| NONE
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
| 1054555339
+
| 1054401633
 
| 2003-05-31
 
| 2003-05-31
|
+
|  
| An inspection of the well site revealed a gas leak and a well incapable of production. There is no surface production equipment or flow lines at the well site. The gas was escaping from the well through a valve at the well head.
+
| received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted.
 
+
|  
Accompanied by J. Hoerst.
+
|  
|
+
| Compliance Notice
| 9-9-05(A)1
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1054555339
 
| 1054555339
 
| 2003-05-31
 
| 2003-05-31
|
+
|  
 
| An inspection of the well site revealed a gas leak and a well incapable of production.  There is no surface production equipment or flow lines at the well site.  The gas was escaping from the well through a valve at the well head.
 
| An inspection of the well site revealed a gas leak and a well incapable of production.  There is no surface production equipment or flow lines at the well site.  The gas was escaping from the well through a valve at the well head.
  
 
Accompanied by J. Hoerst.
 
Accompanied by J. Hoerst.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
| 1054555339
+
| 1443973945
| 2003-05-31
+
|  
|
+
|  
| An inspection of the well site revealed a gas leak and a well incapable of production.  There is no surface production equipment or flow lines at the well site.  The gas was escaping from the well through a valve at the well head.
+
|  
 
+
|  
Accompanied by J. Hoerst.
+
|  
|
+
|  
| NONEH
 
|
 
 
|-
 
|-
 
|-
 
|-
| 1443973945
+
| -243948692
|
+
| 2006-05-26
|
+
|  
|
+
| Gate valve appears to be closed.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 397133036
 
| 397133036
 
| 2008-03-10
 
| 2008-03-10
|
+
|  
 
| Well has good id. Well is capable of production. All production valves are open and wellhead is connected to a main line.
 
| Well has good id. Well is capable of production. All production valves are open and wellhead is connected to a main line.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 467627782
 
| 467627782
 
| 2004-12-04
 
| 2004-12-04
|
+
|  
 
| Passed.
 
| Passed.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -478273780
 +
| 2008-01-29
 +
|
 +
| No id. Well is capable of production. Lines are connected to the wellhead. Valves are open. Equipment looks new. Site has been mowed and is clean.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -71065851
 +
| 2006-05-26
 +
|
 +
| FOLLOW UP TO NOV #  -243948692  Gate valve appears to be closed.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -737133283
 +
| 2008-01-31
 +
|
 +
| Called company and informed them that they need an Id on the well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 20:56, 14 July 2015

Well Details

Well ID: 34-079-20250
Loading map...
County: Jackson
Municipality:
Operator Name: GEOPETRO LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1995-03-05
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 38.93655532
Longitude: -82.62313394

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2005-0 0.0 0.0
2006-0 6576.0 0.0
2007-0 1334.0 0.0
2008-0 79.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 2752.0 0.0
2013-0 507.0 0.0
2014-0 3071.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1054401633 2003-05-31 received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted.
1054401633 2003-05-31 received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted. Compliance Notice
1054401633 2003-05-31 received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted. Compliance Notice
1054401633 2003-05-31 received call from Jackson EMA via ODNR radio room 5/30/2003 23:15 hrs notified of gas leaking from this well. Oak Hill VFD on scene. Arrived on site 9:45 hr this date with Steve Ochs. Found 2 valve coming off the casing leaking significantly. Valve would not shut off any further. Returned to Oak Hill purchased 2 bull plug and installed as tight as possible with 12 wrench. Well is not equiped to produce. No gas line attached, appears to have never been in production. No identification posted. Compliance Notice
1054555339 2003-05-31 An inspection of the well site revealed a gas leak and a well incapable of production. There is no surface production equipment or flow lines at the well site. The gas was escaping from the well through a valve at the well head.

Accompanied by J. Hoerst.

1443973945
-243948692 2006-05-26 Gate valve appears to be closed.
397133036 2008-03-10 Well has good id. Well is capable of production. All production valves are open and wellhead is connected to a main line.
467627782 2004-12-04 Passed.
-478273780 2008-01-29 No id. Well is capable of production. Lines are connected to the wellhead. Valves are open. Equipment looks new. Site has been mowed and is clean.
-71065851 2006-05-26 FOLLOW UP TO NOV # -243948692 Gate valve appears to be closed.
-737133283 2008-01-31 Called company and informed them that they need an Id on the well.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.