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== Well Details == | == Well Details == | ||
{| class="wikitable" width="95%" | {| class="wikitable" width="95%" | ||
− | | Well ID: 051-24519 | + | | Well ID: 42-051-24519 |
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 40.035497, -79.773463 | width=100% | height=100% }} | | style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 40.035497, -79.773463 | width=100% | height=100% }} | ||
|- | |- |
Well ID: 42-051-24519 | Loading map...
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County: Fayette | |
Municipality: Franklin Township | |
Operator Name: CHEVRON APPALACHIA LLC | |
Farm/Lease Name: ROSA UNIT 6H | |
First Permit Date: 2012-10-10 | |
Last Permit Date: 2012-10-10 | |
Spud Date: 2012-10-25 | |
Unconventional: Yes | |
Horizontal: Yes | |
Producing: Yes | |
Violations: None | |
Latitude: 40.035497 | |
Longitude: -79.773463 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
2113258 | 2012-10-26 | No Violations Noted | HORIZONTAL MARCELLUS, ROCKY MOUNTAIN # 1 DRILLING 24" CONDUCTOR CASING @ 120' (10/25/2012). | |
2121755 | 2012-06-13 | No Violations Noted | Pre-op Inspection of well site. Perimeter E&S in place and functioning. | |
2134368 | 2012-12-26 | No Violations Noted | HORIZONTAL MARCELLUS, CROWN # 5 MOVING ON LOCATIOIN THIS WEEK. RIGGING UP DURING INSPECTION (12/26/2012). | |
2134373 | 2012-12-27 | No Violations Noted | HORIZONTAL MARCELLUS, CROWN # 5 DRILLING ON AIR @ 146' (TD).RUNNING WATER PROTECTION CASING AND CEMENTING TODAY. | |
2134376 | 2012-12-31 | No Violations Noted | HORIZONTAL MARCELLUS, CROWN # 5 DRILLING ON AIR @ 239' (TD). RUNNING COAL PROTECTION CASING AND CEMENTING TODAY(12/29/2012). | |
2134378 | 2013-01-04 | No Violations Noted | HORIZONTAL MARCELLUS, CROWN # 5 DRILLING ON AIR @ 2110' (TD). RUNNING INTERMEDIATE CASING AND CEMENTING TODAY(1/4/2013). | |
2134387 | 2013-01-14 | No Violations Noted | HORIZONTAL MARCELLUS, DRILLING ON AIR @ 8218' (TD).DURING FINAL OPERATION DISCOVERED DIRECTIONAL MOTOR AND TRI-CONE BIT LEFT IN HOLE. GOING FISHING TO RETRIEVE THESE TOOLS(1/14/2013). | |
2136971 | 2013-01-23 | No Violations Noted | HORIZONTAL MARCELLUS, CROWN # 5 WENT BACK IN FISHING FOR TOOLS AND RETRIEVED WITH OUT ANY PROBLEMS. CLEANING WELL BORE AND CEMNETING PLUG BACK TO 7200' (1/19/2013).SETTING BRIDGE PLUG AND LOADING HOLE WITH OIL BASE MUD.CAPPING AND MOVING TO NEXT WELL. MOVING TO ROSA # 7 - H (1/21/2013). | |
2139594 | 2013-02-06 | In Compliance with Policy | Operator self reported a spill of Synthetic oil based mud onto containment. Estimated 7 barrels released onto contianment, nothing reached the ground. I visually verified spill on containment. Operator cleaned up and reported spill in compliance with the current Departments spill policy. | |
2139603 | 2013-02-07 | In Compliance with Policy | Operator self reported a release of 7gallons of foam onto containment and 0.5 gallons onto snow covered gravel. I visualy inspected spill site and found no evidence of impacted material. Operator cleaned up and reported spill in compliance with current Departments spill policy. |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2012-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|