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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-067-21470 | | Well ID: 34-067-21470 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 40.41, -81.11 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | | + | | County: [[Harrison_County,_Ohio|Harrison]] |
|- | |- | ||
− | | | + | | Municipality: [[North_Township,_Harrison_County,_Ohio|North Township]] |
|- | |- | ||
− | | | + | | Operator Name: [[EAP OHIO LLC]] |
|- | |- | ||
− | | | + | | Well Pad ID: [[US-OH-001251]] |
|- | |- | ||
− | | | + | | Farm/Lease Name: HARTLEY 2-13-6 |
|- | |- | ||
− | | | + | | License Status: Producing |
|- | |- | ||
− | | | + | | License Date: 2017-07-10 |
|- | |- | ||
− | | | + | | Spud Date: 2017-07-21 |
|- | |- | ||
− | | | + | | Spud Drilling Contractor: [[PATTERSON DRILLING]] |
|- | |- | ||
− | | | + | | Final Drill Date: 2017-09-20 |
|- | |- | ||
− | | | + | | Well Total Depth: 22898.00 ft |
|- | |- | ||
− | | Longitude: -81. | + | | Configuration: Horizontal |
+ | |- | ||
+ | | Latitude: 40.410000 | ||
+ | |- | ||
+ | | Longitude: -81.110000 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | APP | ||
+ | | 2015-04-29 | ||
+ | | Proposed Formations:TRENTON THRU BLACK RIVER, Issued Date:4/29/2015, Expired Date:4/28/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT | ||
+ | |- | ||
+ | | Correction to Well | ||
+ | | 2017-04-14 | ||
+ | | CHANGE TO WELL NUMBER PER OWNER REQUEST. | ||
+ | |- | ||
+ | | APP | ||
+ | | 2017-05-10 | ||
+ | | Proposed Formations:TRENTON-BLACK RIVER, Issued Date:5/10/2017, Expired Date:5/10/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT | ||
+ | |- | ||
+ | | APP | ||
+ | | 2017-07-06 | ||
+ | | Proposed Formations:POINT PLEASANT, Issued Date:7/6/2017, Expired Date:7/6/2019 12:00:00 PM, Drilling unit acres:379.01, Proposed Well Type:OG, Proposed Well Class:POOL | ||
+ | |- | ||
+ | | APP | ||
+ | | 2017-07-10 | ||
+ | | Proposed Formations:POINT PLEASANT, Issued Date:7/10/2017, Expired Date:7/10/2019 12:00:00 PM, Drilling unit acres:379.01, Proposed Well Type:OG, Proposed Well Class:POOL | ||
+ | |- | ||
+ | | Reached Total Depth | ||
+ | | 2017-09-20 | ||
+ | | | ||
+ | |- | ||
+ | | Correction to Well | ||
+ | | 2018-02-16 | ||
+ | | UPDATE TARGET/TAKE PER AS-DRILLED PLAT | ||
+ | |- | ||
+ | | Completion Report Received | ||
+ | | 2018-03-06 | ||
+ | | | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2018-03-17 | ||
+ | | | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 2019-07-10 | ||
+ | | | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | | 2018-03-19 | ||
+ | | style="text-align: right;" | 8400 | ||
+ | | style="text-align: right;" | 8521 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | 2018-03-16 | ||
+ | | style="text-align: right;" | 22650 | ||
+ | | style="text-align: right;" | 22771 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | | ||
+ | | style="text-align: right;" | 22650 | ||
+ | | style="text-align: right;" | 22771 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | | ||
+ | | style="text-align: right;" | 8400 | ||
+ | | style="text-align: right;" | 8521 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | | | ||
+ | | style="text-align: right;" | 8400 | ||
+ | | style="text-align: right;" | 8521 | ||
+ | | style="text-align: right;" | 30 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Perfs Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | | 1 | ||
+ | | 10/25/2017 | ||
+ | | 11/29/2017 | ||
+ | | style="text-align: right;" | 7779 | ||
+ | | style="text-align: right;" | 17,130,000.0 | ||
+ | | style="text-align: right;" | 1,719,690.0 | ||
+ | |- | ||
+ | |} | ||
+ | ==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="22"| 1 | ||
+ | | rowspan="2"| FR-76 | ||
+ | | rowspan="2"| HALLIBURTON | ||
+ | | rowspan="2"| Friction Reducer | ||
+ | | Petroleum Distillate Hydrotreated Light | ||
+ | | 064742-47-8 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.01331 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Proprietary Inorganic Salt | ||
+ | | Trade Secret | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.01331 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| BA-40L | ||
+ | | rowspan="1"| HALLIBURTON | ||
+ | | rowspan="1"| pH Adjusting Agent | ||
+ | | Potassium Carbonate | ||
+ | | 000584-08-7 | ||
+ | | style="text-align: right;" | 60 | ||
+ | | style="text-align: right;" | 0.00021 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| SC-30 | ||
+ | | rowspan="1"| FOUNTAIN QUAIL | ||
+ | | rowspan="1"| Scale Inhibitor | ||
+ | | Sodium Hydroxide | ||
+ | | 1310-73-2 | ||
+ | | style="text-align: right;" | 2 | ||
+ | | style="text-align: right;" | 0.00021 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| BA-40L, BC-140 X2, FE-1A, FR-76, | ||
+ | HAI-OS, OPTIFLO-III DELAYED RELEASE, SP BREAKER, WG-36 | ||
+ | | rowspan="2"| HALLIBURTON | ||
+ | | rowspan="2"| Breaker, Corrosion Inhibitor, Cross Linker, Friction Reducer, Gelling Agent, Iron Control Agent, pH Adjusting Agent | ||
+ | | Non-MSDS Components Not Provided by Supplier | ||
+ | | Not Assigned | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Polyacrylamide copolymer | ||
+ | | Trade Secret | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0162 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Chlorine Dioxide | ||
+ | | rowspan="1"| FOUNTAIN QUAIL | ||
+ | | rowspan="1"| Anti-Bacterial Agent | ||
+ | | Chlorine Dioxide | ||
+ | | 10049-04-4 | ||
+ | | style="text-align: right;" | 1 | ||
+ | | style="text-align: right;" | 0.00016 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Northern White Sand | ||
+ | | rowspan="1"| HALLIBURTON | ||
+ | | rowspan="1"| Proppant - Natural | ||
+ | | Crystalline Silica (Quartz Sand, Silicon Dioxide) | ||
+ | | 014808-60-7 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 16.4008 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| HAI-OS | ||
+ | | rowspan="2"| HALLIBURTON | ||
+ | | rowspan="2"| Corrosion Inhibitor | ||
+ | | Propargyl Alcohol (2-Propynol) | ||
+ | | 000107-19-7 | ||
+ | | style="text-align: right;" | 10 | ||
+ | | style="text-align: right;" | 0.00027 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Methanol (Methyl Alcohol) | ||
+ | | 000067-56-1 | ||
+ | | style="text-align: right;" | 60 | ||
+ | | style="text-align: right;" | 0.00165 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| BC-140 X2 | ||
+ | | rowspan="2"| HALLIBURTON | ||
+ | | rowspan="2"| Cross Linker | ||
+ | | Ethylene Glycol | ||
+ | | 000107-21-1 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.01445 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Monoethanolamine borate | ||
+ | | 026038-87-9 | ||
+ | | style="text-align: right;" | 60 | ||
+ | | style="text-align: right;" | 0.0289 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| 7.5%HCL HYDROCHLORIC ACID | ||
+ | | rowspan="2"| HALLIBURTON | ||
+ | | rowspan="2"| Acid | ||
+ | | Hydrochloric Acid | ||
+ | | 007647-01-0 | ||
+ | | style="text-align: right;" | 8 | ||
+ | | style="text-align: right;" | 0.09118 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Water | ||
+ | | 007732-18-5 | ||
+ | | style="text-align: right;" | 93 | ||
+ | | style="text-align: right;" | 1.12457 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Fresh Water | ||
+ | | rowspan="1"| CHESAPEAKE ENERGY | ||
+ | | rowspan="1"| Carrier/Base Fluid | ||
+ | | Water | ||
+ | | 007732-18-5 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 66.9494 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| FE-1A | ||
+ | | rowspan="2"| HALLIBURTON | ||
+ | | rowspan="2"| Iron Control Agent | ||
+ | | Acetic Anhydride | ||
+ | | 000108-24-7 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 0.0061 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Acetic acid | ||
+ | | 000064-19-7 | ||
+ | | style="text-align: right;" | 60 | ||
+ | | style="text-align: right;" | 0.00366 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="2"| OPTIFLO-III DELAYED RELEASE | ||
+ | | rowspan="2"| HALLIBURTON | ||
+ | | rowspan="2"| Breaker | ||
+ | | Crystalline Silica (Quartz Sand, Silicon Dioxide) | ||
+ | | 014808-60-7 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.00053 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | Ammonium Persulfate | ||
+ | | 007727-54-0 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 0.00176 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Recycled Produced Water | ||
+ | | rowspan="1"| CHESAPEAKE ENERGY | ||
+ | | rowspan="1"| Carrier/Base Fluid | ||
+ | | Water | ||
+ | | 007732-18-5 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 13.7508 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| WG-36 | ||
+ | | rowspan="1"| HALLIBURTON | ||
+ | | rowspan="1"| Gelling Agent | ||
+ | | Guar Gum | ||
+ | | 009000-30-0 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 0.09106 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| SP BREAKER | ||
+ | | rowspan="1"| HALLIBURTON | ||
+ | | rowspan="1"| Breaker | ||
+ | | Sodium Persulfate | ||
+ | | 007775-27-1 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 0.00062 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
|} | |} | ||
− | == | + | For data sources see<ref>{{cite web |
− | {{ | + | | title = FracFocus Fracking Chemicals Database |
+ | | date = 2019-04-02 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-06-19 }}</ref> | ||
+ | == Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | | 2017-10-25 | ||
+ | | H2O | ||
+ | | style="text-align: right;" | 10 | ||
+ | | style="text-align: right;" | 4903 Bbl | ||
+ | | style="text-align: right;" | 359664 | ||
+ | | [[Halliburton]] | ||
+ | | STAGE 1/96 | ||
+ | STAGES 2-95 SEE IMAGES | ||
+ | |- | ||
+ | | 2017-11-29 | ||
+ | | H2O | ||
+ | | style="text-align: right;" | 10 | ||
+ | | style="text-align: right;" | 3719 Bbl | ||
+ | | style="text-align: right;" | 333740 | ||
+ | | [[Halliburton]] | ||
+ | | STAGE 96/96 | ||
+ | STAGES 2-95 SEE IMAGES | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblStimulation Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE EXPLORATION LLC]] | ||
+ | | style="text-align: right;" | 979684 | ||
+ | | style="text-align: right;" | 128157 | ||
+ | | style="text-align: right;" | 354 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[CHESAPEAKE EXPLORATION LLC]] | ||
+ | | style="text-align: right;" | 147946 | ||
+ | | style="text-align: right;" | 17066 | ||
+ | | style="text-align: right;" | 90 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[CHESAPEAKE EXPLORATION LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 59631 | ||
+ | | style="text-align: right;" | 354 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[CHESAPEAKE EXPLORATION LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 2617 | ||
+ | | style="text-align: right;" | 90 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Inspection Date | ||
+ | !scope="col" style="text-align: center"| Inspection Type | ||
+ | !scope="col" style="text-align: center"| Inspection Result | ||
+ | !scope="col" style="text-align: center"| Inspection Comments | ||
+ | |- | ||
+ | | -1813808201 | ||
+ | | 2018-4-10 0:00: | ||
+ | | PL | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -2046503067 | ||
+ | | 2017-9-14 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | -80923220 | ||
+ | | 2016-2-23 0:00: | ||
+ | | ND | ||
+ | | No Violations | ||
+ | | 0.50 | ||
+ | |- | ||
+ | | 0080923220 | ||
+ | | 2016-02-23 | ||
+ | | Not Drilled | ||
+ | | No Violations | ||
+ | | On the day of my inspection accompanied by inspector Mark Moreland, I witnessed the well location has been constructed but the permitted wells have not been drilled and no conductor or tin horn has been set. The pad is fenced and all man doors were locked. The lease road was in adequate condition. | ||
+ | |- | ||
+ | | 0090389048 | ||
+ | | 2017-09-06 | ||
+ | | Casing String Witnessed | ||
+ | | No Violations | ||
+ | | On the day of my inspection I witnessed the surface casing cement job. Patterson 580 drilled a 17.5 inch diameter open hole to a depth of 676 feet. Previous casing set and cemented was 20 inch diameter conductor casing to a depth of 94 feet. Wyoming Casing ran 676 feet of 13.375 inch diameter casing, j-55, 54.5lbs/foot. Casing was centralizer with 6 centralizers. Shoe track is 47 feet long. Schlumberger was onsite with 615 sacks of class A cement. Cement weighed with mudscale at 15.6 ppg and yield of 1.2. 50% excess ran in open hole. Cement displaced with 97 barrels of fresh water. 20 barrels of geland 10 barrels of water pumped ahead of cement. 37 barrels of cement returned to surface, and floats held with .75 barrel back. Mix water has pH of 7, <38 ppm chlorides and 69 degrees Fahrenheit. | ||
+ | |- | ||
+ | | 1020166870 | ||
+ | | 2018-11-06 | ||
+ | | Preliminary Restoration | ||
+ | | No Violations | ||
+ | | On the day of my inspection I witnessed this pad containing 3 producing wells. This well is producing off of natural reservoir pressure through tubing. Surface annular pressure is 31 and intermediate annular is 65. Intermediate annular is plumbed into flowline. Production equipment includes 3 GPUs, 3 sand seperators, 2 compressors, a combustor, and 10 400 barrel steel tanks in their own containment. Six tanks are condensate and four are produced water. Site meets requirements of OAC 1509.072A for preliminary restoration. | ||
+ | |- | ||
+ | | 1500899320 | ||
+ | | 2017-07-24 | ||
+ | | Casing String Witnessed | ||
+ | | No Violations | ||
+ | | On the day of my inspection I witnessed Express energy services had augured a 26 inch diameter hole to 110 feet. Hole and cellar were both comletely full of water. Water was sucked out of cellar. 110 feet of 20 inch diameter conductor casing was run on 7-22-17. Express energy services was onsite with 210 sacks of class A cement. Additives include 2% CaCl and .5 lb./sack floseal. Cement weighed with mudscale at 15.6 ppg and yield of 1.18. 50% percent excess ran. Cement was displaced with 35.5 barrels of fresh water. 15 barrels of cement returned to surface. Job was scheduled at 9 am and water trucks did not arrive on location until 11am. | ||
+ | |- | ||
+ | | 153339106 | ||
+ | | 2020-6-22 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | 1813808201 | ||
+ | | 2018-04-10 | ||
+ | | Preliminary Restoration | ||
+ | | No Violations | ||
+ | | On the day of my inspection I found this pad containing 3 properly labeled well that are producing on natural reservoir pressure. All wells have christmas tree style wellheads. Pressure gauges read as follows: Surface 43 psi, Intermediate 7.5 psi, Production 1129 psi, and Tubing 680 psi. Intermediate annulus is plumbed to buried flowline with dump valve. Blind side of casing hanger is also plumbed into a buried flow line but is currently shut in. Production equipment includes ten 400 barrel steel tanks within their own steel containment, two compressors, two line heaters, three sand separators, three GPUs, two heater treaters, a vapor recovery stack, and a combustor. Site is stable and vegetated. Site meets preliminary restoration requirements of 1509.072A. | ||
+ | |- | ||
+ | | 1992298965 | ||
+ | | 2019-10-23 0:00 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 1.00 | ||
+ | |- | ||
+ | | 2046503067 | ||
+ | | 2017-09-14 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | On the day of my inspection I witnessed Patterson 580 was drilling a 8.5 inch diameter hole at 11,317 feet into the curve. Walk around pad location to view containment and no spills, leaks or hole were noted. Pad drains are shut in. | ||
+ | |- | ||
+ | | 90389048 | ||
+ | | 2017-9-6 0:00:0 | ||
+ | | CS | ||
+ | | No Violations | ||
+ | | 3.00 | ||
+ | |- | ||
+ | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | ==References== | ||
+ | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
+ | [[Category:FracFocus]] |
Well ID: 34-067-21470 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: North Township | |
Operator Name: EAP OHIO LLC | |
Well Pad ID: US-OH-001251 | |
Farm/Lease Name: HARTLEY 2-13-6 | |
License Status: Producing | |
License Date: 2017-07-10 | |
Spud Date: 2017-07-21 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2017-09-20 | |
Well Total Depth: 22898.00 ft | |
Configuration: Horizontal | |
Latitude: 40.410000 | |
Longitude: -81.110000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2015-04-29 | Proposed Formations:TRENTON THRU BLACK RIVER, Issued Date:4/29/2015, Expired Date:4/28/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
Correction to Well | 2017-04-14 | CHANGE TO WELL NUMBER PER OWNER REQUEST. |
APP | 2017-05-10 | Proposed Formations:TRENTON-BLACK RIVER, Issued Date:5/10/2017, Expired Date:5/10/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2017-07-06 | Proposed Formations:POINT PLEASANT, Issued Date:7/6/2017, Expired Date:7/6/2019 12:00:00 PM, Drilling unit acres:379.01, Proposed Well Type:OG, Proposed Well Class:POOL |
APP | 2017-07-10 | Proposed Formations:POINT PLEASANT, Issued Date:7/10/2017, Expired Date:7/10/2019 12:00:00 PM, Drilling unit acres:379.01, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2017-09-20 | |
Correction to Well | 2018-02-16 | UPDATE TARGET/TAKE PER AS-DRILLED PLAT |
Completion Report Received | 2018-03-06 | |
Record Last Modified | 2018-03-17 | |
Construction Permit Expires | 2019-07-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2018-03-19 | 8400 | 8521 | 30 |
2018-03-16 | 22650 | 22771 | 30 |
22650 | 22771 | 30 | |
8400 | 8521 | 30 | |
8400 | 8521 | 30 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 10/25/2017 | 11/29/2017 | 7779 | 17,130,000.0 | 1,719,690.0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | FR-76 | HALLIBURTON | Friction Reducer | Petroleum Distillate Hydrotreated Light | 064742-47-8 | 30 | 0.01331 | 0 |
Proprietary Inorganic Salt | Trade Secret | 30 | 0.01331 | 0 | ||||
BA-40L | HALLIBURTON | pH Adjusting Agent | Potassium Carbonate | 000584-08-7 | 60 | 0.00021 | 0 | |
SC-30 | FOUNTAIN QUAIL | Scale Inhibitor | Sodium Hydroxide | 1310-73-2 | 2 | 0.00021 | 0 | |
BA-40L, BC-140 X2, FE-1A, FR-76,
HAI-OS, OPTIFLO-III DELAYED RELEASE, SP BREAKER, WG-36 |
HALLIBURTON | Breaker, Corrosion Inhibitor, Cross Linker, Friction Reducer, Gelling Agent, Iron Control Agent, pH Adjusting Agent | Non-MSDS Components Not Provided by Supplier | Not Assigned | 0 | 0 | 0 | |
Polyacrylamide copolymer | Trade Secret | 30 | 0.0162 | 0 | ||||
Chlorine Dioxide | FOUNTAIN QUAIL | Anti-Bacterial Agent | Chlorine Dioxide | 10049-04-4 | 1 | 0.00016 | 0 | |
Northern White Sand | HALLIBURTON | Proppant - Natural | Crystalline Silica (Quartz Sand, Silicon Dioxide) | 014808-60-7 | 100 | 16.4008 | 0 | |
HAI-OS | HALLIBURTON | Corrosion Inhibitor | Propargyl Alcohol (2-Propynol) | 000107-19-7 | 10 | 0.00027 | 0 | |
Methanol (Methyl Alcohol) | 000067-56-1 | 60 | 0.00165 | 0 | ||||
BC-140 X2 | HALLIBURTON | Cross Linker | Ethylene Glycol | 000107-21-1 | 30 | 0.01445 | 0 | |
Monoethanolamine borate | 026038-87-9 | 60 | 0.0289 | 0 | ||||
7.5%HCL HYDROCHLORIC ACID | HALLIBURTON | Acid | Hydrochloric Acid | 007647-01-0 | 8 | 0.09118 | 0 | |
Water | 007732-18-5 | 93 | 1.12457 | 0 | ||||
Fresh Water | CHESAPEAKE ENERGY | Carrier/Base Fluid | Water | 007732-18-5 | 100 | 66.9494 | 0 | |
FE-1A | HALLIBURTON | Iron Control Agent | Acetic Anhydride | 000108-24-7 | 100 | 0.0061 | 0 | |
Acetic acid | 000064-19-7 | 60 | 0.00366 | 0 | ||||
OPTIFLO-III DELAYED RELEASE | HALLIBURTON | Breaker | Crystalline Silica (Quartz Sand, Silicon Dioxide) | 014808-60-7 | 30 | 0.00053 | 0 | |
Ammonium Persulfate | 007727-54-0 | 100 | 0.00176 | 0 | ||||
Recycled Produced Water | CHESAPEAKE ENERGY | Carrier/Base Fluid | Water | 007732-18-5 | 100 | 13.7508 | 0 | |
WG-36 | HALLIBURTON | Gelling Agent | Guar Gum | 009000-30-0 | 100 | 0.09106 | 0 | |
SP BREAKER | HALLIBURTON | Breaker | Sodium Persulfate | 007775-27-1 | 100 | 0.00062 | 0 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2017-10-25 | H2O | 10 | 4903 Bbl | 359664 | Halliburton | STAGE 1/96
STAGES 2-95 SEE IMAGES |
2017-11-29 | H2O | 10 | 3719 Bbl | 333740 | Halliburton | STAGE 96/96
STAGES 2-95 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | CHESAPEAKE EXPLORATION LLC | 979684 | 128157 | 354 |
2019 | CHESAPEAKE EXPLORATION LLC | 147946 | 17066 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | CHESAPEAKE EXPLORATION LLC | Brine | 59631 | 354 |
2019 | CHESAPEAKE EXPLORATION LLC | Brine | 2617 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1813808201 | 2018-4-10 0:00: | PL | No Violations | 1.00 |
-2046503067 | 2017-9-14 0:00: | DD | No Violations | 1.00 |
-80923220 | 2016-2-23 0:00: | ND | No Violations | 0.50 |
0080923220 | 2016-02-23 | Not Drilled | No Violations | On the day of my inspection accompanied by inspector Mark Moreland, I witnessed the well location has been constructed but the permitted wells have not been drilled and no conductor or tin horn has been set. The pad is fenced and all man doors were locked. The lease road was in adequate condition. |
0090389048 | 2017-09-06 | Casing String Witnessed | No Violations | On the day of my inspection I witnessed the surface casing cement job. Patterson 580 drilled a 17.5 inch diameter open hole to a depth of 676 feet. Previous casing set and cemented was 20 inch diameter conductor casing to a depth of 94 feet. Wyoming Casing ran 676 feet of 13.375 inch diameter casing, j-55, 54.5lbs/foot. Casing was centralizer with 6 centralizers. Shoe track is 47 feet long. Schlumberger was onsite with 615 sacks of class A cement. Cement weighed with mudscale at 15.6 ppg and yield of 1.2. 50% excess ran in open hole. Cement displaced with 97 barrels of fresh water. 20 barrels of geland 10 barrels of water pumped ahead of cement. 37 barrels of cement returned to surface, and floats held with .75 barrel back. Mix water has pH of 7, <38 ppm chlorides and 69 degrees Fahrenheit. |
1020166870 | 2018-11-06 | Preliminary Restoration | No Violations | On the day of my inspection I witnessed this pad containing 3 producing wells. This well is producing off of natural reservoir pressure through tubing. Surface annular pressure is 31 and intermediate annular is 65. Intermediate annular is plumbed into flowline. Production equipment includes 3 GPUs, 3 sand seperators, 2 compressors, a combustor, and 10 400 barrel steel tanks in their own containment. Six tanks are condensate and four are produced water. Site meets requirements of OAC 1509.072A for preliminary restoration. |
1500899320 | 2017-07-24 | Casing String Witnessed | No Violations | On the day of my inspection I witnessed Express energy services had augured a 26 inch diameter hole to 110 feet. Hole and cellar were both comletely full of water. Water was sucked out of cellar. 110 feet of 20 inch diameter conductor casing was run on 7-22-17. Express energy services was onsite with 210 sacks of class A cement. Additives include 2% CaCl and .5 lb./sack floseal. Cement weighed with mudscale at 15.6 ppg and yield of 1.18. 50% percent excess ran. Cement was displaced with 35.5 barrels of fresh water. 15 barrels of cement returned to surface. Job was scheduled at 9 am and water trucks did not arrive on location until 11am. |
153339106 | 2020-6-22 0:00: | PW | No Violations | 1.00 |
1813808201 | 2018-04-10 | Preliminary Restoration | No Violations | On the day of my inspection I found this pad containing 3 properly labeled well that are producing on natural reservoir pressure. All wells have christmas tree style wellheads. Pressure gauges read as follows: Surface 43 psi, Intermediate 7.5 psi, Production 1129 psi, and Tubing 680 psi. Intermediate annulus is plumbed to buried flowline with dump valve. Blind side of casing hanger is also plumbed into a buried flow line but is currently shut in. Production equipment includes ten 400 barrel steel tanks within their own steel containment, two compressors, two line heaters, three sand separators, three GPUs, two heater treaters, a vapor recovery stack, and a combustor. Site is stable and vegetated. Site meets preliminary restoration requirements of 1509.072A. |
1992298965 | 2019-10-23 0:00 | PW | No Violations | 1.00 |
2046503067 | 2017-09-14 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I witnessed Patterson 580 was drilling a 8.5 inch diameter hole at 11,317 feet into the curve. Walk around pad location to view containment and no spills, leaks or hole were noted. Pad drains are shut in. |
90389048 | 2017-9-6 0:00:0 | CS | No Violations | 3.00 |
For data sources see[10]