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Difference between revisions of "37-063-37124"

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== Well Details ==
 
== Well Details ==
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{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-063-37124
 
| Well ID: 37-063-37124
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 40.496855, -79.210713 | width=100% | height=100% }}  
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| style="height=100%; align=center" rowspan="14" | {{#display_map: 40.496855, -79.210713 | width=100% | height=100% }}  
 
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| Operator Name: [[KEYROCK ENERGY LLC]]
 
| Operator Name: [[KEYROCK ENERGY LLC]]

Revision as of 21:17, 28 June 2014

Well Details

Well ID: 37-063-37124
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Operator Name: KEYROCK ENERGY LLC
First Permit Date: 2011-06-13
Last Permit Date: 2011-06-13
Spud Date: 2011-10-31
Unconventional: No
Horizontal: No
Violations: None
Latitude: 40.496855
Longitude: -79.210713

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 20370.0 365.0 0.0 0.0 0.0 0.0
2012-0 15302.0 365.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1975921 2011-05-26 No Violations Noted review of coal bed methane alt. method
2020364 2011-11-17 No Violations Noted Keyrock had contracted Phillip Drilling (Wayne Braden- Tool Pusher). E&S controls and well sign was present.

No freeboard or E&S issues at the time of inspection. Conductor pipe was installed to 40 feet (9 5/8¿ pipe) and sanded in. Surface pipe was installed to 698 feet (7¿ pipe). Centralizers were set at 87¿, 249¿, 379¿, 493¿, and 618¿. Surface pipe was cemented with 300 sks of Class A with 7 bbls return. Production pipe was set at 1265 feet. Water was encountered at 230¿, 300¿ and 1100¿. Phillips moved off-site to the Tamsula #5.

2021183 2011-11-16 No Violations Noted At the time of inspection, well sign Es plan present. Access road entrance muddy, operator had brush truck removing mud off township road. Access road muddy. Spoke with Keyrock Reps Chris Shea and Doug Wadsworth via telephone while onsite regarding acccess road conditions. Doug Wadsworth expressed intent to haul in rock today to help stabilize access road in order to reduce muddy conditions and the potential for an accelerated erosion event. Rig currently moving to Tamsula 5 well.

Well drilled not yet equipped for prodcution. One below grade pit onsite-- adequate freeboard. Operator plans to dispose of pit contents onsite according to regulation. Filter fence installed below gradient, appears to be maintained and functioning. No accelerated erosion or sedimenation issues noted aside from access road. A follow up will be conducted to ensure roadway is stablized.

References